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4.3L Vortec Lower Intake Gasket Replace and MPFI Upgrade

Sharps40

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So....its been leakin out the top side, slow but steady. Ordered the gaskets and the MPFI upgrade....they came in today and a frost plug let go too. So, can't delay any longer. Wish me luck, its a huge job.

its a 4.3L but the manifold gasket leakage and replacement is about the same on the 5.3 and 5.7. Mostly work with basic hand tools and a real pain. But, fortunately all the connectors for the electronics are different and its about impossible to confuse them and get them in the wrong spot.

So...to the job.

Here....the frost plug on the rear drivers side started weeping today.

i.imgur.com_pt1tXZ4.jpg


And here on the passenger front of the motor, the intake manifold gasket has crumbled (they are plastic and 100% fail between about 100K and 150K miles....mine has 149K). Fortunatly, both leaks are to the outside and not into the oil pan. So, no washed out bearings. The intake gaskets fail to the inside about as often as not, usually destroying bearings before you find out ya got a leak.

i.imgur.com_6EPOtQ2.jpg


First, I removed the air box system and then the throttle body. I'll be doing the throttle body mod (remove the blockage at about 10 oclock on the throttle plate that reduces low and midrange torque since GM surveys determined that folks didn't want lots of power off the line). Clean it up, cut off the offending blockage and reassemble for reinstall tomorrow.

i.imgur.com_KJud7yk.jpg


Once the plastic plenum is removed, I note the original CSFI (Poppet Valve) central fuel injection. Been getting the occasional slow start. This will get replaced with the more reliable MPFI electronic fuel injection which is a standard GM upgrade since there were so many complaints about the unshrouded poppeds gunking up and sticking, etc. CSFI was last used on the Blazers in 2002. This one has 149K on it so, might as well replace it with the better/newer system now. Amazon to the rescue, $160 saved and arrived in 2 days.

i.imgur.com_qYZNG0e.jpg


To get the lower manifold off, remove everything on top. Pull the wiring up and out of the way, loosen the bolt holding the fuel pipes and pull the assembly up out of the way (no need to crack the short lines from the bracket...just blead it down before pulling out the pipes). Remove the coil. Remove the PCV, breather pipes, water neck, heater hoses, EGR, etc. I pulled the alternator for more room and also removed the ac compressor (just lay it out of the way, don't open the pipes), take off fan belt, water pump bypass hose, brake vacuum hose, distributor cap and wires.

Finally, remove about 3 bolts and 3 nuts from the AC/Steering Pump bracket and slide it forward 2" to uncover the one hidden intake manifold bolt on the DS front of the manifold.

i.imgur.com_JALTHZo.jpg


Turn the engine by hand to TDC on the compression stroke. Rotor should point at the triangle on the dizzy base....marked in white. There is no timing adjustment, so the dizzy has to go back in exactly on these marks or it won't run right or at all. Once the dizy is out, do not rotate the engine or the oil pump drive shaft, so that later, you can back the rotor (counter clockwise) up to line up the marks on the lower shaft and drop it right back in the hole. When the marks line up like shown, you'll know its in right and will start and run.

i.imgur.com_o1C1S4f.jpg


Pull the eight bolts that secure the lower manifold to the heads. Yank the manifold and you get to see the crumbling and broken plastic GM gaskets. Even with the radiator/block drained, you'll get some coolant in the valley, that'll have to be mopped out and with all the work, an oil and filter change, immediately, is indicated.

i.imgur.com_Uh8piAe.jpg


i.imgur.com_ZFCbQ3j.jpg


i.imgur.com_su6ZH7N.jpg
 
Cleaned up and the new Fel Pro perminant gaskets sitting in place on the heads. Threaded holes were swarfed out with solvent and a good set of gunbrushes. You can tap them too but will need a long extension for the tap....brush is easier if they are not too cruddy. RTV is used on the front and rear in the valley. And a bit more sopping up coolant to do. Final assembly will be tomorrow. For now, cleaning all the threads on bolts so they can be sealed and properly torqued. While in there I replaced the valve cover gaskets. The plenum and fuel rails will get all new Fel Pro gaskets too, they are in the kit. $20 saved on Amazon for the Fel Pro best kit and again, here in 2 days. They all arrived as I was finishing cleaning up the manifolds!

i.imgur.com_VGdOjNN.jpg


And here, the old style poppet injectors removed and replaced by the Multiport Injector. Follow the directions as #3 has to go behind and over #1 in order for the tubes to fit the plenum without interference.

i.imgur.com_0zZGXc8.jpg


Tomorrow is reassembly and I have to fix the frost plug. Then a 24 hour sit for the RTV to cure and with luck, Monday morning is Fire Up.
 
Started at 0700 this morning, worked till 1530 including cleaning up the tools and garage. Got it all back together and battery back in, no smoke. Did not start it yet. The label on the fel pro RTV for the front and rear of the manifold says 15 minutes to skin, 5 hours to dry, 24 hours to cure. So, can't put the coolant back in till about 0800 Monday. For now, I've triple checked it all and have no left over parts and all the connections are made, hoses and electrical. Also tightened up the two weeping frost plugs....hopefully they will seal otherwise I'll have to dismount the motor.

Removed the gaskets first thing this morning and dry fit the manifold three times to ensure I could hit the guide studs I put in and had all the cables and hoses routed out of the way so the manifold would drop down straight onto the gaskets and rtv at the ends with no smear. Wound up finding that the best position was belly across radiator, feet on garage door.....so, gaskets on and guide studs in place and rtv on the ends....

i.imgur.com_MlvhjeB.jpg


Slipped the manifold right into place without any slippage that could have knocked out the rtv on the ends. After sealing the manifold bolts with white pipe thread sealer, I put some in finger tight and pulled the guide studs and started torqueing the manifold bolts. Three torques, 50, 100 and 144 in lbs in the proper cross sequences and did a final check to ensure all were at 144 in lbs....just for peace of mind.

i.imgur.com_WRPAoMJ.jpg


Stabbed the dizzy, no dice, a tooth off....pulled aligned the lower dimple with the line and stabbed again 17eleven more times, no dice, would not seat except when off mark. Finally got a long screwdriver down in there, rotated the oil pump shaft a scooch clockwise, realigned the dizzy and dropped it in and finally, seated on mark. I'm hopeing I got it right. If not it'll either not start or run rough as a cob....but I have high hopes.....I believe its right. Heres a photo of it seated but off mark....one tooth off and 30 minutes to get it to pick up the right gear tooth and bottom out.

i.imgur.com_e6sdLcc.jpg


Here most of the manifold fittings and electrics and modified throttle body is back in place. I worked back to front in order to ensure I didn't cover up something that needed hooked up!

i.imgur.com_Tzrbnkt.jpg


Everything back in, bolted/torqued/snugged/lubed/sealed, etc. Looks right. 50twenty double checks as I went and upon finishing up. Fixed a broken windshield washer line....no more drip there either. Coolant in the radiator tomorrow morning and I'll turn the key. At least here, with the battery hooked back up, I'm not seeing any smoke!

i.imgur.com_TdMWzLX.jpg


Drivers side rear frost plug that was leaking. The press in plug was replaced with an expandable plug and I put my wrench on the nut,,,,,finger tight. So, snugged it up and the weep stopped. So, we'll see. With luck, and even though this one can be got to without raising the motor, I'd rather try snugging it up for now than replacement. It was only put in this summer when the motor mounts were replaced. Fingers crossed. Close inspection reveled another expansion plug on the Passenger front under the motor mount....and I found a drop of coolant on that motor mount....so......sliding my 3/16" thick open wrench into the 5/16" open slot between the motor mount and the block, I find the nut on the expansion plug.....spend several minutes figuring out upsidedown-rightietighty-leftyloosie and sure enough, it was only finger tight. Gave it a good snugging up. They leak now, its goin to a shop to have the motor lifted out!

i.imgur.com_het6aXq.jpg


I think the hard part now is waitin till the rtv cures so, I'll likely settle back with a couple aspirin for the aches and pains and a good bourbon and a movie till its time to go to the garage again.
 
All done. So far, seems all successful. After a 30 mile test run, it appears to be gas, oil, coolant and vacuum tight.

Got up and went out at 830 (24.5 hour cure on the RTV on the intake ends) and filled Pixie with coolant. Checked for any leaks at the freshly tightened frost plugs and the pesky drain that always weeps on a plastic radiator (I have long since learned to pack the drain threads with a bit of soft setting pipe sealer in addition to its rubber o-ring), and every thing looked good.

With some light trepidation, I got in, set the park brake and turned the key. Two turns and Pixie fired up and settled into cold high idle. Let her run for 45 minutes with the heat on high checking everything for leaks....couldn't find any.

So, took her for a 30 mile run on the highway and noted a high hot idle. Usually she idles along at 650 rpm.....it was up around 750 to 800 and the throttle pedal felt stiff. Otherwise no issues. Check engine light is on but I expected that after replacing so much stuff and having powered it up with the battery install before reconnecting the MAF sensors. It should clear in about 75 miles of driving or several warm/cold cycles. If not, I'll check with the OBD reader at Orielly's.

In the meantime, the combination of MPFI and the throttle body mod made the low range torque come on much better. She no longer works hard to climb the hills out of the neighborhood in lower gears, acceleration is better, idle is smoother and the hot restarts are instant, no lag with the new injectors.

Got back to the house, checked again for leaks and none noted. So....changed the oil and wix filter. I went ahead and switched to 5W30 full synthetic since its a fairly high mileage engine.

I took off the air cleaner hat and looked at the routing of the throttle cable. Had it on the wrong side of the PCV valve assembly adding an extra bend. Put it back where its supposed to be and the throttle freed up. In addition, with the reroute of the cable RPM at hot idle dropped back to a comfortable 700 RPM, only slightly higher than the usual 650ish it used to run.

It seems I got it right.....for now!

--------------

It looks like an unexpected side benefit of switching to Mobile 1 Synthetic oil (5W30) on this high mileage engine is an overall increase of oil pressure.

Regularly, Dinosaur Oil provided me hot readings of 18 psi Idle and 35 psi at Speed.

It would appear that Fake Oil is going to provide somewhat improved figures of 25 psi Idle and 45 psi at Speed.

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250 miles have rolled under Pixie's 10.5" wide tires and she's still idling 900 with an engine light. We idle along in traffic with the brake on to keep it below 30 mph.

So, came home this evening, swarfed out the Idle Air Control slot in the throttle body with carb spray. Some better....so, I did the idle relearn for the 275th time. 800 rpm progress, figured I'd give it another 100 miles and see. So, went hunting in the back yard, killed a doe and on the way to get ice and a cigar its idling 1500 and 1000 and 700 and 1800 and well, we limped home and processed the deer.

Took a shower and thought it over.

Went back out, fired it up, sprayed everything between the fenderwells with carb cleaner and wd40 looking for vacuum leaks. None.

Shut Pixie off and yanked the IAC stepper valve out of the throttle body (had been to oreilly this PM and the single code was P0507, unexpected high idle...yeah, I already knew that. Unfortunatly its a generic Diagnostic code with about 40eleven causes. But my problem weren't on the GM list of causes). Anyway, the IAC valve was a touch cruddy, cleaned it....cleaned the seat, lubed the oring and reinstalled. Started Pixie....700 rpm....great....till I blipped the throttle....Pixie stuck at 1000 rpm.

Scratched my head. Scratched my belly. Scratched my nuts. Could it be?.....

Pulled the air hat, got a flashlight and looked down on the throttle blade I had removed to modify (removal of the blockage to increase low and midrange torque).....

Flipped the throttle plate gently, sticky.....wiped it out...flipped it, sticky....right there at closing sticks but can be forced closed but not under spring power.

Looked close, flashlight, bifocals, knees on radiator head bumpin bottom side of hood....yep, back half of the throttle has a gap as wide as a hair, i.e. not wide at all.

Could it be that frackin simple?

Yep. Loosened the torx screws on the plate, bumped the throttle twice gently so the plate aligned.....retorqued the torx screws and flipped the plate again. No hair line gap on the back half and no sticky throttle.

Got backin the drivers seat, bumped the gas pedal, no sticking! Started Pixie, fired right up, settled in at 550 RPM. Shut down and started again three more times, same result....550 RPM idle.

I think its fixed. Test ride tomorrow and that pesky engine light should reset by itself now.

I'll let ya know.
 
I must have got it right. Pixie has been idling properly since the Thursday evening tweak. Smooth powerful acceleration and fast response with no sticking of the throttle off idle. Idle hot and steady at 550 rpm.

Check engine light stayed on since it was still carrying the P0507 unexpected high idle code in the computer.

Been driving a bit, about 75ish miles and on the way to work this morning the light was still on.

Pulled up to the gate at Fort Bragg, engine at idle and that glaring yellow light goes out.

I love it when a plan comes together.
 
Update. Got the first good miles per gallon calculations since the repairs. Pixie is pulling 19.7mpg combined city/hwy. That's up a bit more than 1.5 full mile per gallon over where she was regularly performing prior to the repairs.

Looks to me like the benefits of mpfi and throttle body mod are very much worth doing on a higher mileage Vortec.
 
Thanks for posting this, I have a 94 Blazer with the 4.3, and it is running like crap. No coolant leaks, but suspect the fuel injection part you just replaced. No power, stalls a lot. My vacuum booster is not working either. Not sure if my engine is original as the fuel injection lines look like the one you removed. I am going to replace mine with the newer mpfi like you have. Great pictures, thanks again for such a relevant post, at least to me!
 
No power stalls a lot. Check for exhaust restriction/cat and then check everything on the engine for vacuum leaks, check dizzy/cap/rotor/wires/plugs, etc. Check the codes too....then go to the intake/fuel spider replacement. The spider is a $200+ (Standard Automotive Co) amazon part, so make sure its whats the crappy performance cause before ya slap a new one in. Big job just to find out it was a plugged cat or bad sensor,... Elilminate cheap/easy first.

Otherwise, Glad to help. 94 is a different gen for the blazer/s10 but the essential bits are likely pretty close to the same. So, as long as you're pulling the plenum (upper intake) to yank the poppet spider and replace it with the MPFI spider.....get the felpro permatorque gaskets and replace everything. The factory intake manifold gaskets will fail....period....if your lucky, they fail to the exterior and you don't corrode the main/rod and cam bearings.

Its only 8 more bolts and removing the dizzy to get the lower manifold out and the gasket kit gives you everything you'll need including valve cover gaskets....whole top end will be done. The full gasket set is about $20 cheaper on amazon than at Oh-really/Autozoid/etc.

I believe it codes as a 5 hour job, but that's probably 2 good mechanics with Magic Wenches sprinkling Boob Gloss on the engine for speed and luck. Figger on at least two long days if you go all the way to the lower intake manifold gaskets and for heavens sake, let the RTV sit a full 24 hours before you start the engine so the billion oil bullets per minute coming off the cam and counter shafts don't push a leak out through the uncured sealant.
 
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